Development Of Low Cost Block Mold For Copper Alloy Casting

Suitable block mold formulations for copper alloy casting have been developed and the formulations used were 25% plaster of paris (POP), 75% silica sand and 31-37% water. Silica sand with a grain size of 106-212 µm was added into dilute suspension of POP and the mixing process was continued until a...

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Main Authors: Siti Zaleha, Mohd Nor, Romzee, Ismail, Sahrim, Ahmad, A. S., Samsudin, Mohd Ikmar Nizam, Mohamad Isa
Format: Article
Language:English
English
Published: Penerbit Universiti Teknologi Malaysia 2016
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Online Access:http://umpir.ump.edu.my/id/eprint/14719/
http://umpir.ump.edu.my/id/eprint/14719/
http://umpir.ump.edu.my/id/eprint/14719/1/Development%20Of%20Low%20Cost%20Block%20Mold%20For%20Copper%20Alloy%20Casting.pdf
http://umpir.ump.edu.my/id/eprint/14719/7/FIST-2016-Development%20Of%20Low%20Cost%20Block%20Mold%20For%20Copper%20Alloy%20Casting1.pdf
id ump-14719
recordtype eprints
spelling ump-147192016-12-21T01:29:51Z http://umpir.ump.edu.my/id/eprint/14719/ Development Of Low Cost Block Mold For Copper Alloy Casting Siti Zaleha, Mohd Nor Romzee, Ismail Sahrim, Ahmad A. S., Samsudin Mohd Ikmar Nizam, Mohamad Isa Q Science (General) Suitable block mold formulations for copper alloy casting have been developed and the formulations used were 25% plaster of paris (POP), 75% silica sand and 31-37% water. Silica sand with a grain size of 106-212 µm was added into dilute suspension of POP and the mixing process was continued until a thick slurry (mixture) was obtained. It has been found that the mixing time of molding materials was highly depended on the type of plaster and optimum slurry viscosity around the diameter of 7.7 – 9.6 cm (slump test) was essential to ensure that the wax pattern could be fully invested. In the dewaxing process, the mold was subjected to the temperature of 170oC for 3 hours and burnout process was effectively achieved by heating the molds at 750oC for 5 hours. The pouring process was successfully carried out without any leakage and it was found that all molds can be easily broken under a force of a hammer. The developed mold also able to produce fully formed of casting without any major defects such as misrun, fin or flash and rat tail, which can be associated with inadequate mold temperature, mold cracks and the separation of mold’s material respectively. Penerbit Universiti Teknologi Malaysia 2016 Article PeerReviewed application/pdf en http://umpir.ump.edu.my/id/eprint/14719/1/Development%20Of%20Low%20Cost%20Block%20Mold%20For%20Copper%20Alloy%20Casting.pdf application/pdf en http://umpir.ump.edu.my/id/eprint/14719/7/FIST-2016-Development%20Of%20Low%20Cost%20Block%20Mold%20For%20Copper%20Alloy%20Casting1.pdf Siti Zaleha, Mohd Nor and Romzee, Ismail and Sahrim, Ahmad and A. S., Samsudin and Mohd Ikmar Nizam, Mohamad Isa (2016) Development Of Low Cost Block Mold For Copper Alloy Casting. Jurnal Teknologi (Sciences and Engineering), 78 (6). pp. 27-33. ISSN 0127-9696 (print); 2180-3722 (online) http://www.jurnalteknologi.utm.my/index.php/jurnalteknologi/article/view/9017
repository_type Digital Repository
institution_category Local University
institution Universiti Malaysia Pahang
building UMP Institutional Repository
collection Online Access
language English
English
topic Q Science (General)
spellingShingle Q Science (General)
Siti Zaleha, Mohd Nor
Romzee, Ismail
Sahrim, Ahmad
A. S., Samsudin
Mohd Ikmar Nizam, Mohamad Isa
Development Of Low Cost Block Mold For Copper Alloy Casting
description Suitable block mold formulations for copper alloy casting have been developed and the formulations used were 25% plaster of paris (POP), 75% silica sand and 31-37% water. Silica sand with a grain size of 106-212 µm was added into dilute suspension of POP and the mixing process was continued until a thick slurry (mixture) was obtained. It has been found that the mixing time of molding materials was highly depended on the type of plaster and optimum slurry viscosity around the diameter of 7.7 – 9.6 cm (slump test) was essential to ensure that the wax pattern could be fully invested. In the dewaxing process, the mold was subjected to the temperature of 170oC for 3 hours and burnout process was effectively achieved by heating the molds at 750oC for 5 hours. The pouring process was successfully carried out without any leakage and it was found that all molds can be easily broken under a force of a hammer. The developed mold also able to produce fully formed of casting without any major defects such as misrun, fin or flash and rat tail, which can be associated with inadequate mold temperature, mold cracks and the separation of mold’s material respectively.
format Article
author Siti Zaleha, Mohd Nor
Romzee, Ismail
Sahrim, Ahmad
A. S., Samsudin
Mohd Ikmar Nizam, Mohamad Isa
author_facet Siti Zaleha, Mohd Nor
Romzee, Ismail
Sahrim, Ahmad
A. S., Samsudin
Mohd Ikmar Nizam, Mohamad Isa
author_sort Siti Zaleha, Mohd Nor
title Development Of Low Cost Block Mold For Copper Alloy Casting
title_short Development Of Low Cost Block Mold For Copper Alloy Casting
title_full Development Of Low Cost Block Mold For Copper Alloy Casting
title_fullStr Development Of Low Cost Block Mold For Copper Alloy Casting
title_full_unstemmed Development Of Low Cost Block Mold For Copper Alloy Casting
title_sort development of low cost block mold for copper alloy casting
publisher Penerbit Universiti Teknologi Malaysia
publishDate 2016
url http://umpir.ump.edu.my/id/eprint/14719/
http://umpir.ump.edu.my/id/eprint/14719/
http://umpir.ump.edu.my/id/eprint/14719/1/Development%20Of%20Low%20Cost%20Block%20Mold%20For%20Copper%20Alloy%20Casting.pdf
http://umpir.ump.edu.my/id/eprint/14719/7/FIST-2016-Development%20Of%20Low%20Cost%20Block%20Mold%20For%20Copper%20Alloy%20Casting1.pdf
first_indexed 2023-09-18T22:18:46Z
last_indexed 2023-09-18T22:18:46Z
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