Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line

A study on Autonomous Maintenance (AM) implementation was conducted for CNC machine at automotive components manufacturing line in order to identify and measure equipment losses related to availability, performance and quality rate. These values were used to determine the overall equipment effective...

Full description

Bibliographic Details
Main Authors: A. R., Razali, M., Ishak, Mohd Azam, Musa, Nazrul Idzham, Kasim, Wan Ahmad Najmuddin, Wan Saidin
Format: Article
Language:English
Published: Trans Tech Publications, Switzerland 2015
Subjects:
Online Access:http://umpir.ump.edu.my/id/eprint/9516/
http://umpir.ump.edu.my/id/eprint/9516/
http://umpir.ump.edu.my/id/eprint/9516/
http://umpir.ump.edu.my/id/eprint/9516/1/Improvement%20of%20Overall%20Equipment%20Effectiveness%20%28OEE%29%20through%20Implementation%20of%20Autonomous%20Maintenance%20in%20Crankcase%20Line.pdf
id ump-9516
recordtype eprints
spelling ump-95162018-01-10T02:10:47Z http://umpir.ump.edu.my/id/eprint/9516/ Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line A. R., Razali M., Ishak Mohd Azam, Musa Nazrul Idzham, Kasim Wan Ahmad Najmuddin, Wan Saidin TJ Mechanical engineering and machinery A study on Autonomous Maintenance (AM) implementation was conducted for CNC machine at automotive components manufacturing line in order to identify and measure equipment losses related to availability, performance and quality rate. These values were used to determine the overall equipment effectiveness (OEE) of the manufacturing line before and after AM implementation. The project started with AM team formation before it was continued with 5S activities and fuguai (abnormality) detection and restoration. Kaizen was used for continuous improvement to restore deteriorated parts and components of the machine. Autonomous Maintenance standards such as cleaning, lubricating and inspection were developed. The AM team members consistently followed the operator maintenance standards to ensure that machine is always in good working condition. The OEE results were taken daily after AM implementation and compared with the data before the implementation. The average OEE result shows significant improvement from 65.8% to 80.4% after the AM implementation. However, the result still did not achieve the company’s target. The main reason was because the machine was very old, which almost reaches deterioration stage according to the bath tub curve. Some recommendations are suggested as to push the OEE value closer to the company’s target including a review on other pillars in Total Productive Maintenance (TPM). Trans Tech Publications, Switzerland 2015 Article PeerReviewed application/pdf en http://umpir.ump.edu.my/id/eprint/9516/1/Improvement%20of%20Overall%20Equipment%20Effectiveness%20%28OEE%29%20through%20Implementation%20of%20Autonomous%20Maintenance%20in%20Crankcase%20Line.pdf A. R., Razali and M., Ishak and Mohd Azam, Musa and Nazrul Idzham, Kasim and Wan Ahmad Najmuddin, Wan Saidin (2015) Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line. Applied Mechanics and Materials, 761. pp. 165-169. ISSN 1662-7482 http://www.scientific.net/AMM.761.165 DOI: 10.4028/www.scientific.net/AMM.761.165
repository_type Digital Repository
institution_category Local University
institution Universiti Malaysia Pahang
building UMP Institutional Repository
collection Online Access
language English
topic TJ Mechanical engineering and machinery
spellingShingle TJ Mechanical engineering and machinery
A. R., Razali
M., Ishak
Mohd Azam, Musa
Nazrul Idzham, Kasim
Wan Ahmad Najmuddin, Wan Saidin
Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line
description A study on Autonomous Maintenance (AM) implementation was conducted for CNC machine at automotive components manufacturing line in order to identify and measure equipment losses related to availability, performance and quality rate. These values were used to determine the overall equipment effectiveness (OEE) of the manufacturing line before and after AM implementation. The project started with AM team formation before it was continued with 5S activities and fuguai (abnormality) detection and restoration. Kaizen was used for continuous improvement to restore deteriorated parts and components of the machine. Autonomous Maintenance standards such as cleaning, lubricating and inspection were developed. The AM team members consistently followed the operator maintenance standards to ensure that machine is always in good working condition. The OEE results were taken daily after AM implementation and compared with the data before the implementation. The average OEE result shows significant improvement from 65.8% to 80.4% after the AM implementation. However, the result still did not achieve the company’s target. The main reason was because the machine was very old, which almost reaches deterioration stage according to the bath tub curve. Some recommendations are suggested as to push the OEE value closer to the company’s target including a review on other pillars in Total Productive Maintenance (TPM).
format Article
author A. R., Razali
M., Ishak
Mohd Azam, Musa
Nazrul Idzham, Kasim
Wan Ahmad Najmuddin, Wan Saidin
author_facet A. R., Razali
M., Ishak
Mohd Azam, Musa
Nazrul Idzham, Kasim
Wan Ahmad Najmuddin, Wan Saidin
author_sort A. R., Razali
title Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line
title_short Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line
title_full Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line
title_fullStr Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line
title_full_unstemmed Improvement of Overall Equipment Effectiveness (OEE) through Implementation of Autonomous Maintenance in Crankcase Line
title_sort improvement of overall equipment effectiveness (oee) through implementation of autonomous maintenance in crankcase line
publisher Trans Tech Publications, Switzerland
publishDate 2015
url http://umpir.ump.edu.my/id/eprint/9516/
http://umpir.ump.edu.my/id/eprint/9516/
http://umpir.ump.edu.my/id/eprint/9516/
http://umpir.ump.edu.my/id/eprint/9516/1/Improvement%20of%20Overall%20Equipment%20Effectiveness%20%28OEE%29%20through%20Implementation%20of%20Autonomous%20Maintenance%20in%20Crankcase%20Line.pdf
first_indexed 2023-09-18T22:08:10Z
last_indexed 2023-09-18T22:08:10Z
_version_ 1777414848053772288